After a few months of repair work, we’re back on the ocean!
Today, we took a few friends for a two hour trip into the Santa Monica Bay.
Our hope was to see some dolphins and maybe catch sight of Minke Whale, but it turned out to be a bit too calm out on the water. On the positive, the winds and waves were minimal… and while wonderful to be on the water, we didn’t have any mammal sightings today.
Another bonus is that two of my new neighbors came to help us park the beast… I felt pretty good parking. It turned out that navigating my way out of this small slip was more challenging than I anticipated. Another neighbor gave me the good advice to wait while reversing until I’m at a full 90 degrees before I start to go forward. No real issues pulling out, but I was treating it more like parallel parking than I needed to…
Trip 1
Fuel
16 of 21 inches
Port
Starboard
Hours
567.8
567.4
Added Eng Oil
0
0
Added Coolant
0
0
Added Transmission Fluid
0
0
Issues
Pretty quickly into the trip, I noticed that our new water temp control was showing we were super hot… like 220 degrees fahrenheit hot. I checked the actual temperature of the port engine and it was running at the same temp as the starboard engine, so I kept monitoring the actual temperature through the rest of the trip, but assumed the sensors hadn’t been isntalled or configured correctly.
On our epic trip down the coast, things went so smooth… the weather was great, the engines purred. The only real issue was when we were traveling around Point Conception, we totally lost steering for a bit. For a few minutes, it was near impossible to turn the steering wheel and then over the next 20 minutes, it became possible to steer, but the steering was extremely jerky.
It turns out, we had likely been driving with a bent rudder the entire time… It may have been bent when we were coming around point conception, but there’s lots of reason to think it was already bent when we left Sacramento. It’s more likely the bent rudder locked up when we hit some kelp… or some similar issue.
When we parked the boat in it’s final home in Marina del Rey, one of my first tasks was to get a diver to look at the rudder and let me know what, if anything, was wrong.
Of course, he came up with a shocked look on his face when he saw the 30 degree bend in the steel shaft and couldn’t believe we were able to drive the boat at all!
So, the next 8 weeks turned into me learning all about rudders and getting to know some old-school boat people in the Long Beach/Wilmington area. In particular, Ryan from the Wilmington Iron Works was just as helpful as could be and sent me in the right direction on a handful of fronts.
Phase 1 – Getting the Rudder Built
The adventure of fixing the rudder started with a recommendation from my uncle that I reach out to Dennis Choate of Diversified Composits. Google shows their business is closed, but I can confirm having been to their shop that they are definitely still in business and building beautiful sailboats. Interestingly, I’m told Dennis was super helpful in giving advice/tips to my grandfather when he was building the boat, so it was a great place to start.
However, after examining the bent rudder, Dennis’s team sent me off to get advice from Ryan Richards of Wilmington Iron Works . They knew he’d be super helpful at telling me if we could fix the rudder or simply needed to get a new one built.
Ryan recommended we build a new rudder from scratch. He worried that if we tried to straighten the steel out on the other rudder, that it wouldn’t be nearly as strong and might not be able to be straightened enough anyway. Plus, he’d have to peal off the fiberglass portion of the rudder regardless in order to straighten the shaft, so we’d have to rebuild the rudder anyway.
The initial idea was to copy the previous rudder completely, which would involve having the team at Wilmington Iron Works build a skeleton for the rudder and then return to Diversified Composits to have them add the fiberglass overlay. However, I asked Ryan to give me a quote on building a steel rudder from steel (no fiberglass), which he did.
In talking with the team at Diversified Composits, they recommended I go with the “all steel” option from Ryan, even though that means I will have two different rudders with different weights (the stainless steel rudder is at least 5 pounds heavier). They assured me the weight difference won’t make a real difference with the size of the Avalon and they were pretty backed up with work, so this would get me a rudder much faster.
Once we agreed to have the new rudder built, things went fast. Within a week, Ryan had a beautiful all-steel rudder built and ready to be picked up, except…
Phase 2 – Getting the notches right
When I was picking up the rudder, Ryan let me know that the original notches were missing two key things… 1) A dimple for the collar bolt to screw into and 2) a keyway for the key to fit into.
Being brand new to these things, it took me at least two conversations with him before I really understood the issue.
It turns out that while my grandfather did so many amazing things with the boat, he somehow avoided a major potential issue when he never added a dimple or keyhole on the original rudders. Especially without the dimple, there was only a bolt against a round stainless steel shaft holding those rudders up for the past 50 years! Plus, without the keyhole, the potential to have the steering arm slip on the shaft was huge (and based on some markings, it seemed clear it had slipped at some point in the past.
It quickly became clear to me that I needed to get the two notches cut into the shaft… However, it was also clear, that it was totally unclear how far up the shaft we need to put the dimple in and how far down we needed the keyway to go.
To solve this issue, we had to have the diver return to put the rudder in, mark it up and then take it out so I could return to Wilmington to have it notched out.
It’s such a tight space, that marking up the rudder for the appropriate dimple (for the collar) was more art than science. The diver would push the rudder up as far as he could go… knock on the bottom of the hull three times and then I’d do my best to measure exactly how far up the post went.
At first we tried to mark everything up with a blank sharpie, but that didn’t last going through the packing glands, so we just marked all the appropriate lengths on a piece of cardboard and marked up the rudder later
Then, when the rudder was out, I’d reverse engineer where the collar would sit, where the dimple needed to be, where the steering arm would sit and where the keyway would needed to be.
What a pain!
Phase 3 – Cuts and more cuts
As part of the process of measuring things, we learned something else… The bow side of the new rudder was about a half-inch too long. In a nutshell, Ryan had built the new rudder to have the same dimensions at the top of the rudder as the old rudder and then he simply did a straight now down parallel to the shaft.
However, my grandfather had designed his rudder to taper down about a half-inch at the bottom…
I’m told that in almost every case, this wouldn’t be an issue as there’s normally about 3 to 4 inches between the bow side of the rudder and the propellers, but my grandfather had designed this set up so that there’s not even 1/2 inch. It’s super tight in there and without the tapering on the bow side of the rudder, the rudder was rubbing against the propeller shaft.
Good news is that we did get it all measured up and I was able to get the rudder back to Ryan. He agreed to taper the new rudder so that it’d fit.
For obvious reasons, we wanted to have the dimple and the keyway cut into the existing starboard rudder as well and Ryan agreed to cut those up as well!
Overall, one of the more painful parts of this process was simply the time things took. It would often take a few days to schedule the diver, a few days for me to have time to drive down to Wilmington and a few days for Ryan to ramp up his team… The result is that it took at least four weeks between the time the rudder was initially built and we were ready to install the two rudders. back in the boat.
Phase 4 – Reinstalling the rudder
Installing the rudder was a bit of a pain mainly because we were doing this while the boat was still in the water. This meant the diver had to push hard on the rudder to get it up enough for the collar to be in position where the screw would fit in the dimple. We really didn’t have but maybe an eighth of an inch extra, so it took a few tries. But once we got a strategy in place for the port side rudder, the starboard side went smoothly.
I was able to get the collar on, then it was simply a matter of aligning the two rudders up so that the steering columns were on correctly.
Of course, there were a ton of small complications (such as breaking both a brass bolt on the steering arm and a brass cotter pin, but those were small issues and relatively easy to resolve.
Worth noting:
The diver was so darn patient, knowledgeable and helpful. If anyone in the Marina del Rey area, ever needs a diver, I highly recommend Steve from Hullworkz.
At some point, I’ll do my best to document out trip down the coast as it was one hell of an epic adventure… but I think I want to start by documenting the issues we’ve fixed as a way to get things down while they’re still relatively fresh in my mind.
In a nutshell, when we were trying to get the boat out Sacramento, we ran into a series of problems, but one problem has turned out to be an expensive blessing-in-disguise.
In a nutshell, we had started both of our 1972 Ford Lehman engines up with no issues a few times and then on the morning we were ready to start our adventures to SoCal, of course one of the engines wouldn’t start.
Mike, the mechanic helping me out, fairly quickly diagnosed that the short-off solenoid was no longer firing, so there was no way to get fuel into the engine.
Of course, trying to find a replacement for a 50 year old solenoid, turned out to be one hell of an adventure and the end result was that we learned from a “Lehman” guy out of Georgia, that my grandpa had put the shut-off solenoid in a particularly bad place to begin with. The Lehman guy predicted that by having it right before the high-pressure injectors, we were likely causing air to get sucked back into the engine every time we shut the engines off…
In a nutshell, the guy from Georgia predicted a key problem that has plagued these engines since the beginning, which is that I’ve heard lots and lots of people bitch about how they constantly need to bleed the engines.
We simply got a hose made that bypassed the solenoid and for the duration of our trip down the coast, we manually shut the engines off via a lever that’s directly on the engine. It’s not ideal to not be able to turn the engines off from the cockpit area, but it was certainly better than trying to solve a problem that didn’t have an obvious solution.
It turns out that once we started shutting the engines off via the lever, we never had to bleed the engines again. Bless his heart for all the amazing work he did on this boat, but one thing my grandfather apparently screwed up was in they placement of the shut-off value.
Once we were settled in Marina del Rey, I tasked a mechanic with add a new shut-off solenoid system… and in this case, it’s a solenoid that physically pulls back the lever that we had been manually using. Here’s what the new shut-off solenoid looks like on the engine.
One thing this required us to do was to add a kill switch to the dashboard.
I really wanted to have the cut-off switch fire when we moved the ignition to “off”, but the mechanics gave me a ton of reasons that this would never be possible. We tried buying a different ignition switch (at their recommendation) that included an “auxiliary” position (to the left of “off”) that was suppose to kill the engine, but this did’t work either. I kinda forget why, but it seems the auxiliary caused the switch to “not” fire… or something odd like that.
Anyway, at the end of the day, the mechanics recommended that we cut two more holes into the dash (one for each engine) and add a push button to kill the engines. That way, it would automatically turn itself back off right after each use and couldn’t be left “on” the kill position. However, I was hesitant to cut into the dash and still not convinced I won’t be able to find a mechanic who can get our new shut-off solenoid to work with the ignition switch.
The end result is that we used two currently unused levers on the dash as our new kill switches (labeled “ENG OFF”).
For people familiar with running the Avalon, I think they should be glad to know that I’m pretty sure we’ve cleared up two long-standing issues that we related to air in the fuel-injectors.
It seems like we don’t have to bleed the engines any more… at least not on a regular basis as I’ve heard from others.
The boat seems to idle really well bow. I also heard complaints that the boat would often turn off at low idle. I suspect that was because there was some residual air in the injectors due to the placement of the shut-off solenoid.
Today, Finn and I came out to the boat with the hope that we’d take it out of the Waves Marina for the first time since we made this the Avalon’s home. However, it was not to be as I needed a first mate to feel comfortable taking it out and our expected first mate didn’t make it.
However, we were able to do a ton of much needed organizing. The key bit of organizing was to separate out the various tools into different buckets, including:
Tape
Bindings, zip ties & clamps
Wrenches/Clamps
Drill bits / Files
Screwdrivers
That has totally cleaned up the toolbox, so it now only has a few items like a hammer and a few key things, such as two (standard) screwdrivers instead of the 50 or so different types that used to be in there and always caused me to wade through a bunch of stuff for the most common tools.
I recently purchased a label maker and it’s encouraged me to go a bit wild on labeling things around the boat.
Outside of some organizational stuff, Finn and I also took the dinghy out for a row.
She took the opportunity to spread the joy of bubbles and…
of course, she very much wanted to row!
Was actually, somewhat hard to get back control of the oars once she got her hands on them!
Earlier this summer, I picked up a boat that was built by my grandfather. He did an amazing job logging every change he made to the boat and I’ve been finding it hard to keep up… but I do love blogging and hoping if I take notes in a more public setting, I’ll be inspired to do a more consistent job…
Also, I’m thinking I’ll go back and republish all of my grandfather’s logs over time. With all the AI tools that can (hopefully) transcribe his writings, it feels like it shouldn’t be all that hard… and would make for a wonderful documentation of everything that’s been going on with the boat.
The plan for the day was to take the boat down to the nearby River View Marina, where Mike wanted to do some final maintenance before we took off on the trip early the next morning. However, after starting the engines and getting ready to go, Mike noticed the power steering wasn’t working.
After more than a bit of sleuthing, we found that a grommet within the power steering shaft had deteriorated… so I spent the afternoon and the next morning driving all over Sacramento in search of the perfect fitting grommet.
Super fortunate that the great team at Tri-C Machinery had two of them. They happily sold me two grommets and even put the steering arm back with their tools, making things fairly smooth.